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Diamond
- Joined
- Feb 20, 2013
- Location
- Houston TX
http://www.practicalmachinist.com/vb/antique-machinery-history/moving-my-new-lathe-274537/\
We got the lathe turned around and moved out of the corner where it was, and pulled about 100 ft. to the shop door. The lathe is waiting for the truck driver to come and move it to its new home tomorrow.
I took a video of us making the 90 degree turn, but when I went to upload it to youtube, I gave up because of the outrageous load time. So the only pictures of the move are the ones of us placing the skids under the lathe. I will take lots up pictures of the lathe being winched onto the truck instead of a video.
The skids are 4 layers of 3/4 in plywood, this was plenty strong on the tailstock end, but a bit light for the headstock.
We had to swing the tailstock out, the pic in the second post shows how far we moved it, to do this my Dad and I just pushed the lathe by ourselves. But when we tried to pull the lathe straight, we couldn't do it. The people that were working in the shop offered to help us with a little 5,000 lb. forklift. We used the forklift to pull and to lift the lathe so we could reset the skates. The forklift handed the tailstock end fine, but strained tremendously when lifting the headstock.
After this we just pulled it straight through an isle way for about 100 ft. This was actually the hardest part because the skates went crazy when they hit the smallest of divots in the floor. And we had to really work to keep the skates in the right direction. This was what the video was about but I don't think I will be able to upload it.
All in all the move went pretty smooth and every thing worked out.
We got the lathe turned around and moved out of the corner where it was, and pulled about 100 ft. to the shop door. The lathe is waiting for the truck driver to come and move it to its new home tomorrow.
I took a video of us making the 90 degree turn, but when I went to upload it to youtube, I gave up because of the outrageous load time. So the only pictures of the move are the ones of us placing the skids under the lathe. I will take lots up pictures of the lathe being winched onto the truck instead of a video.
The skids are 4 layers of 3/4 in plywood, this was plenty strong on the tailstock end, but a bit light for the headstock.
We had to swing the tailstock out, the pic in the second post shows how far we moved it, to do this my Dad and I just pushed the lathe by ourselves. But when we tried to pull the lathe straight, we couldn't do it. The people that were working in the shop offered to help us with a little 5,000 lb. forklift. We used the forklift to pull and to lift the lathe so we could reset the skates. The forklift handed the tailstock end fine, but strained tremendously when lifting the headstock.
After this we just pulled it straight through an isle way for about 100 ft. This was actually the hardest part because the skates went crazy when they hit the smallest of divots in the floor. And we had to really work to keep the skates in the right direction. This was what the video was about but I don't think I will be able to upload it.
All in all the move went pretty smooth and every thing worked out.