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Mazak, Quick Turn 15 T2 The measurements are moving

DeltaMc

Plastic
Joined
Feb 9, 2019
Hello everyone.
We have a Quick turn 15 with T2 control.
Our problem is that every two days or 3 the measurements move 12 mm.
I would like to know if there is any parameter to fix
Thanks in advance
Greetings
 
If the pitch of the lead screw on the axis that moves is 12 mm, the home position is changing.

Possible causes:

Sticky slow down switch.

Crud on switch or cam that operates switch.

Coupling between motor and lead screw has slipped due to crashes, and the marker pulse on the encoder is too close to where the limit switch operates.
I normally set it up to be a half turn from where the switch closes.

Bill
 
12 mm? Wow. You have a mechanical issue, nothing a parameter change will fix. Is it in both X and Z? It may be something as simple as a sticking switch. Make sure it is going to home position correctly. Look at the home return switches at the plus end of your axes. Check for chips or goo and clean them off.
 
I had a simular problem ones.
On my machine the slow down switch was to close to home position so sometimes the ballscrew took an extra turn when homing.
Moved the slow down switch a few mm and all was fine.

But as stated before, also make sure the condition of slow down switch is good.


Ps.
The home function has no switch to indicate home position.
It has an slow down switch and then it turns the ballscrew slowly until the encoder is in the correct angle.
If the slow down switch is in the wrong position it will move the home position by one turn on the ballscrew.
 
Hi.
The 12 mm is on the X-axis, it doesn't mistake me for zero home.
There is another more serious problem, if the energy jumps away if they erase all the parameters..
This is not nice for us
 
Does it move 12mm during the day whithout a restart of the machine?

For the paramater issue you have to replace batteries.
You have 2 or 3 batteries on the boards depending on what version of the harware you have.
The original batteries are 3,6v NiCd batteries but can be replaced by any 3,6v NiMh.
I used holders for 3x1,2v AAA batteries with cabels from the boards to the holders.

If you dont replace these batteries they will leak and destroy the boards

BT2.jpg
 
OK, since I don't know your machine config I'm going to make some guesses. Homing usually works on a switch which gives you approximate position. Indicates you are within 1/2 pitch of the ballscrew of home. From that switch closure it moves, either way is possible depending on your software. When it senses the index pulse (one per rev) it sets home position. A couple of possibilities. The switch is dirty and that makes for uncertainty on when you start the home cycle. More likely is that you are missing the index pulse. Causes could be a weak battery for the encoder, bad connection or the chip logic which senses the index is bad. I'm guessing that the shift in the home position is n*pitch of the ballscrew. I like the idea of Li-mh if you can find the correct voltage but they charge different than the Ni-Cd's. Cleaning the switch with 'LPS' or other contact cleaner may help. HTH
 
Does it change the exact same amount each time? Or just close

Always from 11 to 12.

OK, since I don't know your machine config I'm going to make some guesses. Homing usually works on a switch which gives you approximate position. Indicates you are within 1/2 pitch of the ballscrew of home. From that switch closure it moves, either way is possible depending on your software. When it senses the index pulse (one per rev) it sets home position. A couple of possibilities. The switch is dirty and that makes for uncertainty on when you start the home cycle. More likely is that you are missing the index pulse. Causes could be a weak battery for the encoder, bad connection or the chip logic which senses the index is bad. I'm guessing that the shift in the home position is n*pitch of the ballscrew. I like the idea of Li-mh if you can find the correct voltage but they charge different than the Ni-Cd's. Cleaning the switch with 'LPS' or other contact cleaner may help. HTH

Tomorrow I try to clean the guides, it can be the dirt that creates these problems
 
OK, since I don't know your machine config I'm going to make some guesses. Homing usually works on a switch which gives you approximate position. Indicates you are within 1/2 pitch of the ballscrew of home. From that switch closure it moves, either way is possible depending on your software. When it senses the index pulse (one per rev) it sets home position. A couple of possibilities. The switch is dirty and that makes for uncertainty on when you start the home cycle. More likely is that you are missing the index pulse. Causes could be a weak battery for the encoder, bad connection or the chip logic which senses the index is bad. I'm guessing that the shift in the home position is n*pitch of the ballscrew. I like the idea of Li-mh if you can find the correct voltage but they charge different than the Ni-Cd's. Cleaning the switch with 'LPS' or other contact cleaner may help. HTH

so these pictures tell you how it works on MAzaks. T2 probably doesnt have mask distance parameter to avoid your situation, but T32 has a mask , when machine is jumping ball screw pitch(when dog switch OFF coincides with Z pulse)

the idea is next: when DOG is made and then released , machine should be somewhere in between those Z (one revolution pulse). They (Mitsubishi) give you formula for machine to stop at next Electrical HOME, to do it successfully, that L number must be less then ball screw pitch ( 12 mm ) and more then distance when Servo can actually stop axis (factors like inertia). Then, you have your home position offset and that is where machine stops after Electrical HOME, final stop is MECHANICAL STOP.


so what you do is next: go to machine parameters and make MECHANICAL HOME offset 0 (ZP ), than go to DIAGNOSTIC screen and watch you DOG switch. Move axis manually towards you and then manually towards HOME position. When DOG switch is made and released( record position when it is released) ....say it was 12.4.....then move it towards you again and home it. Now you have to make the difference in between when dog switch is released and home, somewhere around 6 mm. in this case it is guaranty that any fluctuations in DOG limit switch will not affect Z ( one revolution pulse ), and now, after this amazing procedure, you bring your boring bar holder against spindle and clock it with dial indicator. Knowing X axis stroke you now adjust ZP parameter , to make sure you have right X axis stroke.

by the way, it is taken from Mitsubishi M300 CNC control connection manual. Google it and see, it is very well explained.
 

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